Could be that you had residual crud in the tank that's plugging your newly rebuilt carb. Also, 4 turns out is a lot for a mixture screw.
Ride safe,
Alien
Yeah, my thoughts too on the 4 turns out mixture screw.
It's not plugging, quite the opposite, it floods.
There is an inline filter on the gas line.
I found the problem on that though:
It's due to
crappy rebuild workmanship.
Initially the float was set
way too high out of adjustment, causing the fuel to run out the throat. Luckily it's on a "down hill" slope to the Airbox, not into the engine!
Once I fixed that it still leaked a tad bit, running out the overflow hose.
The seat (of the "needle and seat") fits into a "cylinder" built into the carb housing with an O-ring in a grove on the outside of the seat. The seat is held in place with a plate that's screwed down.
The inside of the "cylinder" had debris built up which was preventing the O-ring from sealing.
It took time (you know, like 5 minutes) but I was able to take crocus cloth and clean it up to where, even with the
old O-ring, it seals.