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Author Topic: Loss of one cylinder  (Read 3302 times)
TrapperAH1G
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Posts: 204

Toledo, WA


« on: April 03, 2025, 11:34:17 PM »

Riding on twisties and noticed bike wasn't running right, sluggish.  Pulled over and in checking it out, found that pulling the plug wire on the left front cylinder doesn't change how it runs.  Definite change in idle if I remove any of the other five wires.  From this, I assume the coil should be ok since the second plug wire has spark.  Changed plug, no joy.  Plug wire?  How hard is it to remove ends and replace just the wire?

Thanks for your thoughts, wisdom.
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Jims99
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Posts: 809


Ormond Beach Fl.


« Reply #1 on: April 04, 2025, 04:26:40 AM »

Pull the plug, stick it back on the wire, lay it against metal and start the bike. You will be able to if it’s firing or not. The area can be changed but not sure how difficult that is. Butch Fowler and wood butcher make up coil packs with new wires even in different colors. May also be a clogged float (sticking) not getting fuel. You can’t try running a strong dose of B-12 or Techron to try clear it out.
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The light at the end of the tunnel, is a train.
99 tourer
00 interstate
97 standard
91 wing
78 trail 70
98valk
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Posts: 13518


South Jersey


« Reply #2 on: April 04, 2025, 05:05:32 AM »

Riding on twisties and noticed bike wasn't running right, sluggish.  Pulled over and in checking it out, found that pulling the plug wire on the left front cylinder doesn't change how it runs.  Definite change in idle if I remove any of the other five wires.  From this, I assume the coil should be ok since the second plug wire has spark.  Changed plug, no joy.  Plug wire?  How hard is it to remove ends and replace just the wire?

Thanks for your thoughts, wisdom.

the wire is attached to the coil with a plastic compression tube fitting like this but not brass
https://automation-renew.blogspot.com/2013/02/compression-tube-fittings.html

the wires are stranded cooper, and there is a metal spike inside the coil end that the cable is pushed onto.    
the plug end actually has a removable resistor. there have been some reported cases of one failing.  

from some research yrs ago the carburetor Honda engines all had the same coil/wire setup.

do an ohm check on the plug, it might be bad. 

A nice performance mod I did yrs ago and which I need to reinstall this yr is re-installing the hotter firing blackbird coils.
« Last Edit: April 04, 2025, 05:43:54 AM by 98valk » Logged

1998 Std/Tourer, 2007 DR200SE, 1981 CB900C  10speed
1973 Duster 340 4-speed rare A/C, 2001 F250 4x4 7.3L, 6sp

"Our Constitution was made only for a Moral and Religious people. It is wholly inadequate to the goverment of any other."
John Adams 10/11/1798
h13man
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Posts: 1771


To everything there is an exception.

Indiana NW Central Flatlands


« Reply #3 on: April 04, 2025, 05:08:31 AM »

Well I have fouled two stock NGK's on my bike at two different times both times the plugs were just over 10,000 mi. on two different cylinders.
If you look in the OEM manual, 8,000 mi. change intervals. After the last time I installed NGK Iridium as they really perform great cold starting to the point I only use the "enrichner" at spring roll out only. I have 12,000 on them at this time. Basically getting all I can out of them as I keep a spare in the tool kit.

BTW, there a PDF floating around here somewhere showing how to rebuild the wires using stock components. I used the following:

https://www.speedwaymotors.com/Red-7mm-Solid-Core-Spark-Plug-Wire-20-Ft-,5117.html?sku=91064011&utm_medium=CSEGoogle&utm_source=CSE&utm_campaign=CSEGOOGLE&gclid=Cj0KCQiAhs79BRD0ARIsAC6XpaVH24FToirTU7ukZyHMQuJiYQA7Vg0Z1KagAcFw2BPccdhc5HUqLBkaAkvkEALw_wcB
« Last Edit: April 04, 2025, 05:16:46 AM by h13man » Logged
John Schmidt
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Posts: 15240


a/k/a Stuffy. '99 I/S Valk Roadsmith Trike

De Pere, WI (Green Bay)


« Reply #4 on: April 05, 2025, 05:04:27 PM »

You said no spark on #2(left front), do you have spark on #1...right front? Both fired by the same coil, the one near the front tucked under the tank on the left. I'd just raise the tank enough to get at the wires and check for bad/loose connections for the plug wires. Then check continuity on the #2 wire, you may have a bad resistor which is inside the rubber plug cover.
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TrapperAH1G
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Posts: 204

Toledo, WA


« Reply #5 on: April 05, 2025, 09:54:38 PM »

Number 2 cylinder is the only one that seems not to change the idle when disconnected.  Changed the plug, no improvement.  Played around with the wire, connector and it cured it......for a while, then it lost power again.  Will check for spark tomorrow.

I run techron in my tank every 3rd tank or so.
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da prez
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Posts: 4365

Wilmot Wi


« Reply #6 on: April 06, 2025, 07:30:10 AM »

  I just had one that was a coil break down. We gave the coil to a shop that knew how to test.
 I tried to find the OHMS test , but couldn't come up with the numbers.
  They said it would break down under load. Replaced the coil and all is good.

                                          da prez
« Last Edit: April 07, 2025, 07:44:29 AM by da prez » Logged
TrapperAH1G
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Posts: 204

Toledo, WA


« Reply #7 on: April 13, 2025, 12:17:34 AM »

Finally got a day that wasn't windy and rainy.  Removed the tank, thinking I'd trim the wire at the coil, then change the plug wire if that didn't work.  As soon as I looked at the coil I saw that the ground wire nut was almost all the way backed off.  Tightened it down, put the tank on and connected the lines, fired up and all is good.  No idea why that nut was loose, the other ground wire nut on that coil was tight.

Thanks for all the input, suggestions.  Ride safe.  Tomorrow, Sunday, am riding with my son and grandson.
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Hook#3287
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Posts: 6469


Brimfield, Ma


« Reply #8 on: April 13, 2025, 06:07:18 AM »

Glad it was an easy and cheap fix cooldude

Can't remember hearing of this issue before.
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TrapperAH1G
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Posts: 204

Toledo, WA


« Reply #9 on: June 10, 2025, 06:32:55 PM »

Well, Deja Vu.  Happened again, same cylinder.  No loose connections this time.  Getting spark to cylinder, has compression. Gas in carb bowl.  Plug not fouled, switched with another cylinder and it runs fine, while #2 is still "idle".  Have a couple of friends coming tomorrow to help.  Will keep you posted, feel free to contribute thoughts.
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TrapperAH1G
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Posts: 204

Toledo, WA


« Reply #10 on: June 11, 2025, 06:14:42 PM »

Today, a friend and I worked on the bike.  Cutting to the chase, we determined it wasn't getting fuel at idle but was at higher rpm.  So, removed the intake manifold tubes on 2 and 4, removed bowl on #2 and then took out the jets.  Main jet was clear, idle jet (38S) was totally blocked.  Took almost half an hour using carb cleaner, very small wire and air to clear.  Put it all back together and it does better at idle but isn't totally cured. 

I'm running B12 thru it, letting it sit for a few hours, repeating.  Thinking with the jet closed I may have varnish/build up farther back.  Time will tell, but at least I can now tell a difference when I pull the plug wire at idle.

Oh, I now know someone in the past has changed the idle jets from 35S.  Mains are still 100's.
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Joe333x
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Posts: 144


Boston


« Reply #11 on: June 12, 2025, 04:01:57 PM »

Today, a friend and I worked on the bike.  Cutting to the chase, we determined it wasn't getting fuel at idle but was at higher rpm.  So, removed the intake manifold tubes on 2 and 4, removed bowl on #2 and then took out the jets.  Main jet was clear, idle jet (38S) was totally blocked.  Took almost half an hour using carb cleaner, very small wire and air to clear.  Put it all back together and it does better at idle but isn't totally cured.  

I'm running B12 thru it, letting it sit for a few hours, repeating.  Thinking with the jet closed I may have varnish/build up farther back.  Time will tell, but at least I can now tell a difference when I pull the plug wire at idle.

Oh, I now know someone in the past has changed the idle jets from 35S.  Mains are still 100's.
B12 is good stuff, hopefully clears up the issue for you. Also having a colortune is a great tool to see the combustion in the chamber so you know if you have space and makes tuning a breeze. They seem to be out of stock but maybe you can order one if you call.
https://www.freedomracing.com/g4171-colortune-for-12mm-spark-plug.html?___store=default&srsltid=AfmBOopKZjEluVCg6aoNt6g396L-PXqjqAyHkBkQy_1ujJ2C0Rcqh3NZ-zs&gQT=2
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TrapperAH1G
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Posts: 204

Toledo, WA


« Reply #12 on: July 03, 2025, 08:12:51 PM »

Update:  NO real improvement.  Been using B12, even used Lucas cleaner & Seafoam.  There is no change to idle when I remove the plub wire, BUT, get it to 2000 rpm and there's a noticeable change in sound and a drop in rpm when the wire is removed.  Truly seems just the lower rpm's are involved.  So, if the slow jet is clear, any opinions on what would be the cause?

Thanks.
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Pluggy
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Posts: 415


Vass, NC


« Reply #13 on: July 04, 2025, 05:32:22 AM »

Old Honda coils can create "on-again, off-again" problems.  It is possible cylinder #2 side of the coil can fail and #1 is OK.  I removed the coils on a 4 cylinder Honda to find both plastic cases had cracked.  The eBay replacements have worked fine.

Before you dump more solvent (and money) into the gas tank, consider a replacement set like this:

https://www.ebay.com/itm/145786137878?chn=ps&norover=1&mkevt=1&mkrid=711-166974-028196-7&mkcid=2&mkscid=101&itemid=145786137878&targetid=2274951440814&device=c&mktype=pla&googleloc=9010069&poi=&campaignid=22079117232&mkgroupid=170385470061&rlsatarget=pla-2274951440814&abcId=10150408&merchantid=5089702184&geoid=9010069&gad_source=1&gad_campaignid=22079117232&gbraid=0AAAAAD_QDh949p7p18B2teoViFhVl_ya4&gclid=Cj0KCQjw953DBhCyARIsANhIZoYOj7xGFyf8UTnXMJV-TIz2Kj0rEP9aC9bIe91J9CWMPm_e5vFlZzAaAlS4EALw_wcB

It is not particularly expensive.

If you prefer,  try exchanging the 1-2 coil and wires with the 3-4 set and see if the problem moves with it.  Thats a lot of work.
« Last Edit: July 04, 2025, 06:30:58 PM by Pluggy » Logged
TrapperAH1G
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Posts: 204

Toledo, WA


« Reply #14 on: July 20, 2025, 07:28:08 PM »

Have a spare parts bike, 2000 Standard.  I'll take a coil from it and swap, just to see.  Thinking I may have to rebuild this carb, so will do all at that time.  Went to Red Eye site and didn't see any kits for this, and didn't see where I could order final drive O rings either.  Left a message.
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Pluggy
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Posts: 415


Vass, NC


« Reply #15 on: July 21, 2025, 04:43:01 AM »

Just in case the plug wire is bad.... If that parts bike coil has the cables attached, you can install those along with the coil.
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TrapperAH1G
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Posts: 204

Toledo, WA


« Reply #16 on: July 21, 2025, 08:05:13 PM »

Thanks, already used the plug wire on the parts bike to see if it helped, no joy.  Not expecting the coil to be it, think it's the carb.
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HayHauler
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Posts: 7202


Pearland, TX


« Reply #17 on: July 22, 2025, 06:12:02 AM »

Thanks, already used the plug wire on the parts bike to see if it helped, no joy.  Not expecting the coil to be it, think it's the carb.
Following this.

Hay  Cool
Jimmyt
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98valk
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Posts: 13518


South Jersey


« Reply #18 on: July 22, 2025, 06:41:41 AM »

 dielectric grease on the plug connection? should be none
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1998 Std/Tourer, 2007 DR200SE, 1981 CB900C  10speed
1973 Duster 340 4-speed rare A/C, 2001 F250 4x4 7.3L, 6sp

"Our Constitution was made only for a Moral and Religious people. It is wholly inadequate to the goverment of any other."
John Adams 10/11/1798
Mooskee
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Posts: 573


Southport NC


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« Reply #19 on: July 22, 2025, 02:19:08 PM »

Update:  NO real improvement.  Been using B12, even used Lucas cleaner & Seafoam.  There is no change to idle when I remove the plub wire, BUT, get it to 2000 rpm and there's a noticeable change in sound and a drop in rpm when the wire is removed.  Truly seems just the lower rpm's are involved.  So, if the slow jet is clear, any opinions on what would be the cause?

Thanks.
It sounds like a slow circuit blockage. You seem to have cleared it partially by cleaning the jet. The B12 in time may clean it up.

There is also a possibility of a blockage in the pilot circuit. Using a proper "D" shaped tool for Honda pilot jets, turn the pilot on the offending cylinder 1/2 turn open (CCW). Run the bike and try to get fuel moving through the circuit. If it clears, then set the pilot needle back 1/2 turn in. It is worth a try. You may not get everything out, but the B12 may do the rest.

You can buy a Motion Pro adjusting socket for about 12 bucks. I put it in a 1/4 drive socket. I actually have a flat spot ground on the socket as a reference when adjusting. Amazon has them.

You may need to pull the intake riser off the offending cylinder to get to the pilot easier. If so, stuff a rag in the intake so you don't drop anything into the cylinder.

Of course if you have the appropriate long handled adjuster you can just open the pilot 1/2 turn with it much easier.

Hope this is helpful.
« Last Edit: July 22, 2025, 05:12:14 PM by Mooskee » Logged

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